Stroker rebuild
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Yes im inclined to agree with you Les.
Although I am still leaning towards a 440 conversion, way I see it is, any engine I get is going to of done a few miles and be in need of some work one way or another so I might as well go the whole hog and drop a biggun in.
Although I am still leaning towards a 440 conversion, way I see it is, any engine I get is going to of done a few miles and be in need of some work one way or another so I might as well go the whole hog and drop a biggun in.
Petty Roadrunner 416 Stroker 4 Speed
*MMA-609*
"Built to be driven!"
Why me???
*MMA-609*
"Built to be driven!"
Why me???

I can see your train of thought, however, a 360 block with a 4.180 crank kit = 426ci, with your heads worked a bit, and all your other parts + decent cam you'll easily be in BB territory, 500+ easy HP, 550ftlbs and it'll all bolt up to your trans....just a thought.
Wish you all the best with whatever you do.
Les
Wish you all the best with whatever you do.
Les
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Sounds tempting I must admit and I could write 426 c.i on the bonnetLes Szabo wrote:I can see your train of thought, however, a 360 block with a 4.180 crank kit = 426ci, with your heads worked a bit, and all your other parts + decent cam you'll easily be in BB territory, 500+ easy HP, 550ftlbs and it'll all bolt up to your trans....just a thought.
Wish you all the best with whatever you do.
Les


Petty Roadrunner 416 Stroker 4 Speed
*MMA-609*
"Built to be driven!"
Why me???
*MMA-609*
"Built to be driven!"
Why me???

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- Posts: 1667
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its not necessarily an old slapper of an engine.
yes the block will be less robust but jings most of them have lost wall thickness due to corrosion anyway.
It didn't go into pin holes when bored last time
Thats a good sign.
1)If the piston to bore clerance was too tight a hone and a clean up of those pistons might put it just right. (thats time rather than money spent)
2) its way past what chrylser determined was a safe rebore for their worst case scenario casting, but we don't know if this was a worst case scenario casting, could have been a thick walled casting.
3) you don't need to get it sonic tested to get an indication, an idea, a very good guess, of how poor or good the wall thickness is
4) nobody is suggesting ploughing good money after bad into it. it currently needs time and some head gaskets.
Yes rockers are necessary but the rockers are necessary due to previous breakage for any small block you buy so buying rockers was a given
you can get an indication of whether the bore is particularly thin by doing this
this is a decent "looking for a thick walled block in a breakers yard" method
1) find a core plug in each bank of cylinders that when removed will give you access to the gap between them
2) remove the core plug (new core plug set is about 15 quid and you only need 2 so someone probably has a few to spare)
3) using a screw driver/small file or a dowel in a drill sawed halfway up and wrapped in emery, clean up the crud between the cylinders
4) ram a wedge of feelers in there. call that measuremnet G for gap
5) measure as best you can from the near side of the left bore to the near side of the right bore call that D for distance (do it 5 times and average out what you get to cover off using the verniers on a curved surface errors)
6) we want to work out WT, Wall Thickness
(D-G)/2 = wall thinkness
granted it gives no idication of thickness anywhere else and does not cover core shift
but thats why we have sonic testing
so
take off the water pump (new gasket)
this gives access to a decent area of the bottom of at least 1 the front 2 cylinders.
the place they corrode most is usually around the bottom, if the engine stood
check how bad it is. chip off the crap and look how much has gone.
you can mesure from the water pump face hlf way up and at the bottom and subtract one from the other to get an idea of how much tinner it is at the bottom. you might be able to do it further up as well
based on resserach i did a while ago when looking at hemi 6s
i'd suggest 0.165 wall would be the minimum you'd want on a motor when your plans do NOT involve forced induction
1/4 of an inch would be nice:)
some guys running around with 0.125 but i guess not on stroker motors.
Dave
yes the block will be less robust but jings most of them have lost wall thickness due to corrosion anyway.
It didn't go into pin holes when bored last time
Thats a good sign.
1)If the piston to bore clerance was too tight a hone and a clean up of those pistons might put it just right. (thats time rather than money spent)
2) its way past what chrylser determined was a safe rebore for their worst case scenario casting, but we don't know if this was a worst case scenario casting, could have been a thick walled casting.
3) you don't need to get it sonic tested to get an indication, an idea, a very good guess, of how poor or good the wall thickness is
4) nobody is suggesting ploughing good money after bad into it. it currently needs time and some head gaskets.
Yes rockers are necessary but the rockers are necessary due to previous breakage for any small block you buy so buying rockers was a given
you can get an indication of whether the bore is particularly thin by doing this
this is a decent "looking for a thick walled block in a breakers yard" method
1) find a core plug in each bank of cylinders that when removed will give you access to the gap between them
2) remove the core plug (new core plug set is about 15 quid and you only need 2 so someone probably has a few to spare)
3) using a screw driver/small file or a dowel in a drill sawed halfway up and wrapped in emery, clean up the crud between the cylinders
4) ram a wedge of feelers in there. call that measuremnet G for gap
5) measure as best you can from the near side of the left bore to the near side of the right bore call that D for distance (do it 5 times and average out what you get to cover off using the verniers on a curved surface errors)
6) we want to work out WT, Wall Thickness
(D-G)/2 = wall thinkness
granted it gives no idication of thickness anywhere else and does not cover core shift
but thats why we have sonic testing
so
take off the water pump (new gasket)
this gives access to a decent area of the bottom of at least 1 the front 2 cylinders.
the place they corrode most is usually around the bottom, if the engine stood
check how bad it is. chip off the crap and look how much has gone.
you can mesure from the water pump face hlf way up and at the bottom and subtract one from the other to get an idea of how much tinner it is at the bottom. you might be able to do it further up as well
based on resserach i did a while ago when looking at hemi 6s
i'd suggest 0.165 wall would be the minimum you'd want on a motor when your plans do NOT involve forced induction
1/4 of an inch would be nice:)
some guys running around with 0.125 but i guess not on stroker motors.
Dave
The Greater Knapweed near the Mugwort by the Buckthorn tree is dying
You would need a complete 360 stroker kit with I-beam rods, KB slugs at around $1100 = £680 +ship, + a block, and all the rest you have. Cannot use your crank, wrong main journal size for 360.
example:-
http://www.ebay.com/itm/CHRYSLER-360-40 ... 0809199712
Forged pistons and crank:
http://www.ebay.com/itm/CHRYSLER-360-40 ... 0809199981
Many kits about though.
Les
example:-
http://www.ebay.com/itm/CHRYSLER-360-40 ... 0809199712
Forged pistons and crank:
http://www.ebay.com/itm/CHRYSLER-360-40 ... 0809199981
Many kits about though.
Les
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