I spent Sunday on the car and, well, i have good and bad news to report. Mostly bad tho
I fixed the 2nd leak from the filter, then stripped the carb. Lots of crap in there, probably flushed through from the pipes. I gave the metering blocks and bowls a good swill and blasted every orifice with the airline. I found the float height on the BG website and tweaked that, they were only 1/16" out at most. I don't know how to set any other adjustments on the carb or what to set anything to so that might be an issue...
I left the reg at 7psi- everything i've read recommends that.
Mick-
Yes, fresh fuel.
What's a reluctor?
How do i check for vac leaks? I have the pipe blocked at both ends.
I got it all back together, tried to start it- nothing. No fuel pressure at the pump! I banged, it, shook it, nothing. Up-turned it and opened it up, all seemed fine. Lowered it below the fuel level, out comes fuel... Put it back together and it works fine now

Airlocked somehow?
Anyway, fired the car up. 3-4 pumps of the throttle and it starts easy, this time i wound the throttle stop screw in a bit so it's racing a bit but at least it kept running! Now it's smoking like hell from the oil filter area- The oil filter adaptor plate was leaking so i cut a paper gasket and siliconed it up. The oil filter is a bugger to tighten once the headers are on so it leaked again! Now it's too hot and slippery to tighten so i spent ages cleaning it and had to use a strap but now i'm scared of overtightening it
I started it again an fannied around trying to get the timing. It's doing around 1500-2000 rpm (no revcounter yet), below that it stalls so I can't check initial timing really as that's not exactly idling?
There seems to be a lot of petrol running into the carb mouths but I don't know if thats normal?
It runs fastest around 35-45* and stalls if i go much below or above that. It's so noisy and smoky it's hard to concentrate and i'm doubting myself cos i'm not sure i believe what i'm seeing... then MORE smoke pours out from the filter area! I got under there with a torch cos i was sure i'd stopped the leak this time and it's bloody PETROL leaking from the reg onto the header and turning to steam
Boy i got out from under the car quick!!!
I fixed that leak and decided to quit, i also realised Jasper left the fans disconnected and things were getting a bit hot.
So... I fitted my prop loop. Ah, how I needed that little achievement!
Though this led me to find another little 'issue', the exhausts and the gearbox crossmember are gonna be fighting over the same space...take a look at the pic...
I may even end up with side exits as there's so little room around the 4-link and axle.
I'm not going to start the engine again until the wiring is finished and the damn thing's home.
I'll figure out if i can tweak the x-member and exhausts or if I have to replace them.
I'll replace the float seals.
I'll go through the timing again from scratch.
I don't think i want to see it again for a few days
