I found that i had problems getting the box back in on mine
due to the pilot bush and input shaft not being totally aligned, tool, wooden dowel and screw driver handle all pressed into service
i found that no matter how well I aligned the clutch plate the box was still at the wrong angle due to the shifter housing hitting the tunnel in all positions apart from fully home. i ended up having to droop the engine down at the back to get it in as far as possible, this has its own problems becasue the engine is no longer parrallel to the floor and of course your jack is running across the floor with the box on it. you must also watch for impact on clutch z bar. yes they work at odd angles but go too far and it will come of
once on, twist box back and forth (they are top heavy...this was not easy covered in oil) to align bolt holes
put long bolts in to hold it steady on the jack.
adjust engine height at bell housing to match as much as possible the angle the box was now at when sitting on a jack, this involves 2 jack twiddling in harmony
then I used my crook lock to press the clutch down and leave it pressed
a lot of swearing and shaking the box and i could guide it in and do up the bolts the last 1/2 inch.
but that makes it sound easy
i had to chock the box front face at the bellhouseing with ring spanners to get the open gap the same all round then adjust the jacks and the bolts , this was the easiest way to make incremental changes to the alignment in order to get it onto the shanked well fitting sections of the bolts
clutch plate must have been slightly out even after the 3rd attempt
pressing the clutch allowed movement of plate and input shaft but due to the bolts all in a good few turns and the heads nipped up ( following removeal of spanners) did not allow it to swing way out of a alignment.
your problems get worse if the input shaft has any play, it shouldn't have much or any in a rebuilt box but tiny movement there translates to waggling the tail shaft housing about quite a bit before you actually move the tip of the input shaft in relation to the pilot bearing
1/2 hour job took about 3
next time i'm sure it will be fine......ha...
next time i won't do it alone, in a hurry, the night before the NATS
mines a single rail box your's has shift rods, not only is it top heavy it will have minimal clearnce on the drivers side.
i'm not what you would term weak but i'll admit i aint the strongest fella in the world either
try to avoid the situation where you are bench pressing the box into position, even my little one is a heavy cast iron bugger,
the day you put the box in is always a day when gravity is much stronger
notice how easy it came out...
i also found that after all the pushing and shoving i appeard to have moved the engine and box closer to the radiator
so i ened up loosening everything off at the mounts
levering the box and motor back to the middle of the slots in the mounts
so i didn't put may radiator into fan danger zone..
if i was doing this more than once every couple of years i'd invest in a pit/lift and a transjack...
or just take the lot out as a complete motor and box unit
not the most fun...in fact sticking a red hot needle into a black thumb nail would be more fun, by quite a margin
Dave