
It wasn't bad at all inside, just hardened gaskets from age and some crud washed through from the fuel pipes.
I've tried to i.d. the carb but i think it's a bit of a hybrid, Holley didn't make a 750 vac sec with 2 corner idle screws, 2 metering blocks and no choke horn. The only problem is that i was short a couple of gaskets in the rebuild kit, luckily the old ones were good.
I checked the floats were good too.
It's now all back together, baseline adjustments done and ready to refit.
In case anyone's interested...
Primary jets are .072, Sec .086
Idle mix screws 1 1/4 turns out.
Squirter pump 30cc, jet 31
Throttle blades 172
Power valve 65